From our experiences, the added safety is wonderful but, as with all technologies, there are times when they malfunction. On a few different occasions, we have experienced misfires when the cartridge is thrown into the blade thus ruining both parts even though there was no foreign material to trigger the reaction. One of these occasions happened during our class last week. And thus began the saga.
In this particular instance, it was a partial misfire so the cartridge was lodged into the blade and both were still locked into their place inside the saw. So, out came the crowbar amongst other tools to try and slide these things out of the saw whilst still being attached to each other. Although this was not the easiest of tasks, Jeff managed to wiggle the two pieces out and replace them (luckily we have spares for both) so the class could continue with enough usable table saws.
We sent SawStop the used cartridge and they were able to confirm it was a misfire and not a finger-saving attempt.
As you can see, I removed the switch box side cover and replaced the old D-sub connector with the new one. Then, I ran the cable through the
machine undoing and redoing the clamps that hold it in place throughout the inside of the cabinet. The best part about this task is that it's nearly impossible to see each of the small clamps so, I had to rely on my sense of touch to locate, unscrew, place, and rescrew the cable into the clamps.
From there, the cartridge connector needed to be placed into it's bracket. The bracket is found in a vertical plate below the saw blade where the cartridge lives when it's being used. Even with my child-sized hands, it took some incredible effort to use the Allen wrench to turn the screw whilst holding the lock nut behind. It was a Lohr Woodworking staff group effort to reach both sides of that plate. Tilting the saw back and forth, relying heavily on flashlights, and crawling under, on, and around the saw finally did the trick.
The final step was to use three tiny screws to put the circuit board into place. The afternoon ordeal came to a close when I pulled out the old cartridge cable, reassembled the splitter knife holder, put a new cartridge and blade in, and flipped the "on" switch. A sigh of relief came when the little green light illuminated but, the real test was turning the sucker on and hoping the brand new cartridge didn't fire because of a circuit chip disconnect that I had missed.
The moment of truth came and went as the blade spun perfectly. I am a long way from being a woodworking master but, I'll admit to a self-administered pat on the back for figuring out this high-tech machine. My relationship with the table saws just got a bit more intimate as I now (sort of) understand their inner workings. Thanks to SawStop for saving fingers and limbs on a daily basis but, moreso for giving me a really intricate and mechanical project to expand my brain this week.
It may seem like more work, but next time a similar trip happens, pull the fence, right side table, cast iron table and wings off the saw. It will save you a lot of grief.
ReplyDeleteI maintain the S'stop for an organization called the Artisan's Asylum. A Maker Space in Somerville Mass.. I recently pulled all those items off our saw to do a thorough inspection, lubrication, tune up and maintenance job. I was glad I did, since many of the lube points I needed to get access to were crazy difficult places to get at.
G. Savage
Thank you so much for the advice! You are right in saying that getting at some of the parts is crazy difficult! I will certainly remember this the next time we are faced with such a dilemma and/or need to tune up the machine(s).
DeleteNice Blog. Thanks for sharing with us. Keep Sharing!!
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